The Problem. Some time ago, I came across a project by a team of five operators and supervisors of a factory that manufactures florescence tubes for commercial buildings. The process of manufacturing these tubes were a heavy investment, and so the production volume must be high enough to recoup the investment cost.
One of the expensive ingredients used in the manufacturing process is a powder mix used to coat the interior walls of the florescence tubes. These are sprayed like a shower as the tube envelopes the nuzzles. Immediately after that, the tube is vacuumed and then sealed. All these are done with high precision and high speed mechanical robots in clean room conditions. The tubes produced were of superb quality and last a very long time.
One day, while studying the material purchasing order slip, the engineers noted that the coating powder was very expensive, in fact more expensive than gold, if compared ounce-for-ounce. If only they can just reduce a fraction of a gram for each tube, the savings will be tremendous, given the high volume. The team of five set to work with this in mind.
The Alternatives.
Alternative 1. Use less powder. Obviously, having a thinner coat of powder will reduce material cost and that will save money. Unfortunately, there is a threshold. Anything less, will result in in-complete coverage, and lead to rejects at the end of the inspection station, and this is very costly if rework had to be done.
Alternative 2. Use substitutes. The brightness and durability are the product advantage, and the powder (phosphor++) has ben designed through lengthy research and studies. Another product is in the pipe-line, and all these is outside the purview of the Production Department. Production is in no position to recommend change of material unless they can suggest a substitute and clearly Production Department has no alternative substitute material.
Alternative 3. The Chinney Brush! The team focus on how to reduce the overall usuage of the expensive powder, and the idea of re-cycling came to their team discussion session. They studies the production to find out where there was splurges etc. They found that, some of the rejected tubes had ‘extra volume of powder’ especially around the electrodes. These interfere somewhat and eventually gives abnormal readings when tested on the current flow measuring device and had to be rejected.
Maybe, excessive powder should be removed before sealing the electrode! One member thought of his baby’s milk bottle cleaner, and another the chinney brush.
After a few versions of modification and trails, in less than 4 months, the new automated brush was ready to be installed in all the stations. A simple three brush strokes, remove excess ‘phosphor powder’, and these were recollectd at the end of the production shift and treated before recycling. The projected savings for that year came up to a neat S$100,000!! Not too bad for the team of five.
Learning Point.
Sometimes, the ‘gold dust’ is flying out the window right under our noses. Just look around, think a bit, measure a bit, and there are many things we can improve.













